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1.
针对不锈钢焊接接头存在残余应力且分布不均匀、容易发生应力腐蚀的问题,采用激光冲击强化对其进行处理,探究激光功率密度和冲击次数对表面残余应力状态的优化作用,并通过应力腐蚀试验验证优化效果。结果表明:随着功率密度增加,表面残余应力明显下降,但下降幅度逐渐减小,功率密度4.24GW/cm2与2.83GW/cm2冲击产生的残余应力相差不大,熔合区还存在残余拉应力,说明高功率密度不足以消除表面残余拉应力;随着冲击次数增加,残余拉应力显著降低,2.83GW/cm2冲击3次之后,残余拉应力完全消除,局部最高应力梯度从54.7 MPa/mm下降到11.7 MPa/mm,获得了高数值、分布均匀的残余压应力层。激光冲击强化后,焊接试样的应力腐蚀断裂时间提高了33.48%,激光冲击强化产生的残余压应力是其应力腐蚀抗性提高的重要原因。  相似文献   

2.
强激光冲击铝合金改性处理研究   总被引:15,自引:2,他引:13  
吴边  王声波  郭大浩  吴鸿兴 《光学学报》2005,25(10):352-1356
利用新型聚偏1.1-二氟乙烯(PVDF)压电传感器,实现了对激光引发的冲击波压力的实时测量,得到激光引发的冲击波峰压在铝中成指数型的衰减规律;观测了不同约束层材料在铝靶表面产生的激光冲击波,研究了不同约束层对冲击效果的影响;最后用激光冲击强化装置对7050-T7451航空铝合金结构材料进行了冲击强化处理,对试件激光冲击区存在的残余压应力及位错密度进行了测量。结果显示经激光冲击处理的试件表面具有极高的残余压应力,可达-200MPa以上。激光冲击处理后铝合金的位错密度得到显著的提高,疲劳寿命提高到175%~428%。这些重要结果对激光冲击改性处理技术的实际应用具有指导性作用。  相似文献   

3.
 利用高功率钕玻璃激光器对7050铝合金表面进行了冲击处理,保持泵浦功率不变,用压电传感器和示波器测试了激光冲击产生的压力波形,用X射线应力测量仪测量了激光冲击后铝合金表面的残余应力,并用非接触式光学轮廓仪分析了激光冲击后铝合金的表面形貌,研究了放大自发辐射强度对激光冲击处理7050铝合金冲击压力、残余应力和粗糙度影响的微观机理。研究结果表明:在泵浦功率不变前提下,放大自发辐射强度的增大降低了激光冲击波压力,铝合金表面残余压应力也随之降低,同时铝合金表面粗糙度增大。  相似文献   

4.
针对激光冲击强化铝合金焊缝过程中存在多场耦合导致残余应力变化幅度大、实时表征难的问题,采用ABAQUS非线性有限元软件建立了激光冲击强化7075-T6铝合金板材焊接件的有限元模型,模拟计算焊缝在激光冲击强化前后的残余应力场分布,重点分析了激光冲击强化对焊缝的横、纵向残余应力场的影响规律,并对焊缝的激光冲击强化工艺参数进行优化。研究结果表明,焊缝表面为残余拉应力场并且分布不均,激光冲击强化使得焊缝的拉应力状态转变为高幅压应力状态;优化激光冲击强化工艺参数(如激光能量、激光光斑尺寸、搭接率),可以明显改善焊缝区域和热影响区的残余应力分布;当激光光斑搭接率为50%至70%时,残余应力分布趋于均匀,可以有效消除"残余应力洞"现象。  相似文献   

5.
研究了激光冲击强化对回转半径为350mm大耕深旋耕刀残余应力的影响,利用ANSYS对旋耕刀进行理论应力分析,发现应力集中在刀柄外弯角处,同时进行了激光冲击强化模拟,得到理论残余应力引入值。利用X射线衍射法对激光冲击强化前后旋耕刀表面进行了残余应力测试。结果表明,ANSYS模拟激光冲击强化引入的残余应力值与试验实测的结果吻合得较好,相比未经处理的旋耕刀,激光冲击强化后刀具表面残余应力明显增大,最大残余压应力达412.25 MPa,增幅达166%,残余压应力的引入可消除旋耕刀工作的应力集中,提高了刀具使用寿命。研究结果为进一步提高和优化大耕深旋耕刀制造工艺提供了新的参考依据。  相似文献   

6.
为研究激光冲击对E690高强钢激光熔覆修复层微观组织的影响,选用专用金属粉末对E690高强钢试样预制凹坑进行激光熔覆修复,并使用脉冲激光对激光熔覆层进行冲击强化处理,同时采用扫描电镜、透射电镜和X射线应力分析仪分别对激光冲击前后激光熔覆层的微观组织和表面残余应力进行检测。结果表明:激光熔覆修复后,激光熔覆层组织为等轴晶,熔覆层与E690高强钢基体之间冶金结合良好,其表面残余应力为均匀分布的压应力。经激光冲击后,激光熔覆层截面晶粒得到细化,并观察到大量的形变孪晶,互相平行的孪晶界分割熔覆层粗大晶粒,在激光熔覆层的晶粒细化过程中发挥着重要作用;试样表层位错在{110}滑移面上发生交滑移,在晶界周围形成了位错缠结。经激光冲击后,激光熔覆层冲击区域表面残余压应力数值相较于冲击前提升了1.1倍。  相似文献   

7.
为了使激光冲击强化技术能较好地应用于TC6钛合金的发动机叶片,对TC6钛合金进行试验研究。通过X射线衍射仪、透射电子显微镜等测试技术分析了不同参数下TC6钛合金的微观组织变化,用显微硬度计和残余应力测试仪分别表征表层硬度和残余应力变化,并测试材料冲击后的振动高周疲劳性能。试验结果表明:激光冲击材料后表面组织得到明显细化,随着冲击次数的增加,先后出现了高密度位错、位错胞、亚晶和纳米晶。性能方面,表面硬度在冲击一次即可提高19%,硬度影响深度达到700 m;与此同时表面残余应力最高达到-608.5 MPa,在500 m深度上仍具有-100 MPa左右的应力存在。经三次冲击后,标准疲劳试片的疲劳极限提高近20%。  相似文献   

8.
采用了TIG对核聚变用316LN奥氏体不锈钢进行焊接,并对焊接接头进行了焊后热处理,利用光学显微镜、扫描电镜分析手段研究了焊后热处理对焊接接头微观组织和力学性能的变化。试验结果表明,焊缝中为奥氏体组织,并未发现第二相析出物存在。焊后热处理对接头的拉伸性能影响不大,均断裂在母材位置,但显著提高了接头的延伸率。接头低温冲击试验也展现了良好的抗低温冲击性能。断口分析发现,接头呈韧性断裂。  相似文献   

9.
采用了TIG对核聚变用316LN奥氏体不锈钢进行焊接,并对焊接接头进行了焊后热处理,利用光学显微镜、扫描电镜分析手段研究了焊后热处理对焊接接头微观组织和力学性能的变化.试验结果表明,焊缝中为奥氏体组织,并未发现第二相析出物存在.焊后热处理对接头的拉伸性能影响不大,均断裂在母材位置,但显著提高了接头的延伸率.接头低温冲击试验也展现了良好的抗低温冲击性能.断口分析发现,接头呈韧性断裂.  相似文献   

10.
利用高功率Nd:YAG激光对不同工艺处理的SWOSC-V弹簧钢丝进行单点冲击处理,用X射线应力分析仪测量弹簧内外侧、侧表面的残余应力并计算出残余主应力,建立了激光冲击SWOSC-V弹簧钢丝表面残余应力的产生模型,并利用该模型分析了弹簧钢丝表面残余应力产生的原因。结果表明:弹簧钢丝在经激光冲击处理的表面强化区产生残余压应力,钢丝退火后直接激光冲击处理与经喷丸强化的钢丝激光冲击处理的表面残余应力变化不同,喷丸强化所引起的材料硬化是激光冲击处理弹簧钢丝残余应力变化不同的原因。  相似文献   

11.
Mechanical properties of engineering material can be improved by introducing compressive residual stress on the material surface and refinement of their microstructure. Variety of mechanical process such as shot peening, water jet peening, ultrasonic peening, laser shot peening were developed in the last decades on this contrast. Among these, lasers shot peening emerged as a novel industrial treatment to improve the crack resistance of turbine blades and the stress corrosion cracking (SCC) of austenic stainless steel in power plants. In this study we successfully performed laser shot peening on precipitation hardened aluminum alloy 6061-T6 with low energy (300 mJ, 1064 nm) Nd:YAG laser using different pulse densities of 22 pulses/mm2 and 32 pulses/mm2. Residual stress evaluation based on X-ray diffraction sin2 ψ method indicates a maximum of 190% percentage increase on surface compressive stress. Depth profile of micro-hardness shows the impact of laser generated shock wave up to 1.2 mm from the surface. Apart from that, the crystalline size and micro-strain on the laser shot peened surfaces have been investigated and compared with the unpeened surface using X-ray diffraction in conjunction with line broadening analysis through the Williamson-Hall plot.  相似文献   

12.
Fretting-fatigue is an important factor influencing service life of turbine blades. The present paper describes laser shock peening of potential crack nucleation site in the root region of steam turbine blade for its enhanced service life. The experimental study, performed with an in-house developed 2.5 J/7 ns Nd:YAG laser demonstrated that laser peening introduced a residual surface compressive stress of ?260 to ?390 MPa. Case depth of laser peened surface layer was found to be more than 900 μm.  相似文献   

13.
Four mechanical surface treatments have been considered for the application to austenitic stainless steel structures. Shot peening (SP), laser shock peening (LSP), ultrasonic impact treatment (UIT) and water jet cavitation peening (WJCP), also known as cavitation shotless peening (CSP), have been applied to 8 mm thick Type 304 austenitic stainless steel coupons. This study considers the merits of each of these mechanical surface treatments in terms of their effect on the surface roughness, microstructure, level of plastic work and through thickness residual stress distribution. Microstructural studies have revealed the formation of martensite close to the treated surface for each process. Residual stress measurements in the samples show compressive stresses to a significantly greater depth for the LSP, UIT and WJCP samples compared to the more conventional SP treated sample.  相似文献   

14.
近年来,激光增材制造技术(3D打印)成为科学研究及工业应用领域的热点。为了研究激光冲击强化对增材制造TC4钛合金性能的影响,本文采用能量为5 J,波长为1 064 nm,脉宽为10 ns,光斑直径为3 mm的脉冲激光对3D打印TC4钛合金进行激光冲击强化,分析了激光冲击强化前后材料的显微硬度、显微组织、残余应力以及高温氧化性能。结果表明,经过激光冲击强化后,材料的显微硬度比激光冲击强化前提高了8%,影响层深度达到0.4 mm,强化区域的晶粒得到细化,位错增多,并产生形变孪晶;激光冲击强化的残余压应力数值高达472 MPa,材料的高温抗氧化性能也得到改善。  相似文献   

15.
Effects of hydrogen charging on the stress corrosion cracking (SCC) behavior of 304 and 310 stainless steels under sustained load were investigated in boiling 42% MgCl2 solution. The cracking was accelerated by the incorporation of hydrogen into the steel without altering the crack growth mechanism. The fact that the active dissolution is almost unaffected by the hydrogen charging and tensile stress indicates that the phenomenon of hydrogen-promoted SCC is unlikely a result of hydrogen-facilitated active dissolution. In contrast, hydrogen significantly promotes anodic dissolution in the potential range where the active-to-passive transition occurs. The electrochemical noise detected in the SCC process implies that the crack propagation process is discontinuous and hydrogen charging can raise the frequency of film breakdown at the crack tip. These observations suggest that the hydrogen-promoted SCC may result from the hydrogen-induced passivity degradation.  相似文献   

16.
17.
The influence of a laser shock peening mechanical surface treatment on 2050-T8 aluminum alloy has been investigated, mostly using Scanning Kelvin Probe Force Microscopy. Volta potential difference maps around Al(CuFeMn) precipitates were performed before and after laser-shock peening to determine the influence of laser treatment versus galvanic coupling near precipitates, and resulting pit initiations. It has been shown that laser shock peening either preserves or reduces precipitate-matrix Volta potentials gradients, which in this later case, and correlated to recent corrosion electrochemical investigations, could explain corrosion improvement obtained after laser-shock peening treatments of aluminum alloys. The influence of crystal orientation and plastic deformation, and more specifically the effect of laser-induced compressive residual stresses or work-hardening, on the Volta potential values and on the pitting corrosion behavior was also addressed.  相似文献   

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