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基于重球触地实验的空区塌落振动分析及治理
引用本文:仪海豹,张西良,杨海涛,李明,高琪琪,金科.基于重球触地实验的空区塌落振动分析及治理[J].爆炸与冲击,2019,39(7):88-100.
作者姓名:仪海豹  张西良  杨海涛  李明  高琪琪  金科
作者单位:中钢集团马鞍山矿山研究院有限公司,安徽马鞍山243000;金属矿山安全与健康国家重点实验室,安徽马鞍山243000;中钢集团马鞍山矿山研究院有限公司,安徽马鞍山243000;中国科学技术大学中国科学院材料力学行为和设计重点实验室,安徽合肥230026;金属矿山安全与健康国家重点实验室,安徽马鞍山,243000
基金项目:国家重点研发计划(2017YFC0602902)
摘    要:根据相似理论,以重球落地实验模拟采空区坍塌进而指导采空区治理为出发点,在振动波动特性分析的基础上,分别开展了质量为4 kg和10 kg的重球从1.0、1.5和2.0 m的高度落地的峰值振动速度测试实验;首次提出了累计振动速度衰减率和相对能量比概念;以普氏拱理论为基础,分析了采空区坍塌振动速度。研究表明:振动速度与重球质量和落地高度成正相关,且前者对累计衰减率的影响大于后者;随着测点距离的增大,振动速度整体表现为衰减趋势;重球质量为4 kg和10 kg时,在水平距离重球落地点3.0 m处的累计衰减率分别为79.79%~81.61%和79.95%~83.52%。不同介质交界面的反射和折射可引起振动速度的小幅度“跃增”。重球质量对振动能量衰减影响明显;质量越大,近区能量衰减越慢。采空区冒落体582.5~5 926.5 t,引起的振动速度远大于边坡安全允许值。采用“采空区顶板崩落+边坡削坡”方案进行治理后,边坡安全系数可达到1.26,消除采空区安全隐患。

关 键 词:重球触地实验  振动速度  采空区治理  数值分析
收稿时间:2018-04-20

Goaf collapse vibration analysis and disposal based on a experiment of heavy ball touchdown
YI Haibao,ZHANG Xiliang,YANG Haitao,LI Ming,GAO Qiqi,JIN Ke.Goaf collapse vibration analysis and disposal based on a experiment of heavy ball touchdown[J].Explosion and Shock Waves,2019,39(7):88-100.
Authors:YI Haibao  ZHANG Xiliang  YANG Haitao  LI Ming  GAO Qiqi  JIN Ke
Institution:1.Sinosteel Maanshan Institute of Mining Research Co. Ltd., Manshan 243000, Anhui, China2.CAS Key Laboratory of Mechanical Behavior and Design of Materials, University of Science and Technology of China, Hefei 230026, Anhui, China3.State Key Laboratory of Safety and Health for Metal Mines, Manshan 243000, Anhui, China
Abstract:Based on the similarity theory,the heavy ball landing experiments were conducted to simulate the collapse of the goaf in order to provide guidance for the goaf disposal.The particle peak vibration velocities corresponding to the balls with the mass 4 kg and 10 kg dropping from 1.0,1.5 and 2.0 m respectively were measured experimentally on the basis of characteristics analysis of vibration wave.For the first time,the concepts of cumulative attenuation rate of vibration velocity and relative energy ratio were proposed.The collapse vibration velocity of the goaf was analyzed with the help of the Protodyakonov’s arch theory.The study shows that the mass and dropping height of the heavy ball are positively related to the vibration velocity,and the former has greater influence on the cumulative attenuation rate than that of the latter.With the increase of measuring distance,the overall vibration velocity shows an attenuation trend.The accumulative decay rates for 4 kg and 10 kg heavy balls at 3.0 m are 79.79%81.61%and 79.95%83.52%,respectively.Reflections and refractions at the interface of different media can cause a small“jump increase”in vibration velocity.The mass has a significant effect on vibration energy attenuation:the greater the mass,the slower the energy attenuation in the near area.The goaf collapsed mass is 582.5 t to 5 926.5 t and it causes the particle vibration velocity to be much larger than that of the safety allowable value.With the comprehensive treatment plan of“roof caving+slope slope cutting”,the slope safety factor can reach 1.26,completely eliminating the hidden dangers in the goaf area.
Keywords:heavy ball touchdown experiment  vibration velocity  goaf disposal  numerical analysis
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